Day 23
Monday
28 January 2013
We have tested the frisbee launcher and have discovered issues with the stability of the wheels when moving at full rpm.
The hopper and drivetrain systems are complete. We are waiting to test the drivetrain and have it driving as soon as possible.
We are set to complete the entire robot build by the end of week 4, this Saturday, and begin troubleshooting/final testing.

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