Day 24
Tuesday
29 January 2013
We successfully tested the frisbee launcher. We have isolated the stability issues of the Frisbee launcher. The issue is with the wheels itself. Alternative wheels are being sought for the issues. The frisbee feeder for the launcher/hopper will be completed by tomorrow.
We tested the connectivity between the cRio and the laptop/controls. We will have the drivetrain driving by tomorrow.
We are preparing for the final integration of all systems for the robot. The superstructure design is being finalized. We have an idea for how we will integrate all of the systems. We are waiting for the completion of all systems before proceeding with the final integration.

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